2021 – Remedial Works To Lock and Weir One – It seemed like a good idea in the design office

Christopher Dann, Chad Martin, Garry Fyfe, Nigel Rutherford

This paper presents a case study on remedial works that were undertaken at Lock and Weir One
along the River Murray, that to our knowledge are the first of their kind in Australia.
The weir structure’s left abutment is comprised of a stepped concrete structure founded on timber
piles, with timber sheet piles extending beneath the structure to cut off seepage through underlying
alluvium. A piping incident occurred at the left abutment in late 2014 and a filter blanket was
installed as an emergency response measure. A detailed review of historic construction documents
showed that there was a “missing” timber sheet pile upstream of the piping boil. Geotechnical
investigations, including piezometer installation confirmed the missing timber sheet pile was the
likely cause of the piping incident. A piping risk assessment showed the residual risk of further piping
was reasonably high.

A range of remedial works was considered as permanent risk reduction works. However, these
solutions required extensive temporary works to expose the missing timber sheet pile including a
cofferdam to access the defect and partial demolition of a recently constructed fishway structure.
An alternate Secant ‘Grout Column’ solution was developed that comprised targeted drilling and
backfill grouting to close the gap where the sheet pile was not installed and to grout an inferred void
under the abutment structure. This solution was successful at reducing seepage through the
abutment structure, as indicated by monitoring piezometers.

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